Why is EVERYONE complaining about a tight fit with V8's in the M37 engine bay??
I stuffed this big block Hemi into the M37, Don't know why there are so many issues with the size of the engine bay.
Blown Chryco Hemi in an M37
Moderators: Cal_Gary, T. Highway, Monkey Man, robi
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- CPL
- Posts: 128
- Joined: Sat Oct 28, 2017 6:07 pm
Blown Chryco Hemi in an M37
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- Hemi in M37 2 (1).jpg (132.99 KiB) Viewed 1970 times
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- hemi in M37 (1).jpg (110.18 KiB) Viewed 1970 times
Re: Blown Chryco Hemi in an M37
any motor that small has to be a Wankel.
NV
NV
Re: Blown Chryco Hemi in an M37
That's really clever, Outpost! I was all hyped up to see that install; however it was worth the laugh when I saw the pictures!
Gary
Gary
Cal_Gary
1954 M37 W/W
MVPA Correspondent #28500
G741.org Forum member since 2004
1954 M37 W/W
MVPA Correspondent #28500
G741.org Forum member since 2004
-
- CPL
- Posts: 128
- Joined: Sat Oct 28, 2017 6:07 pm
Re: Blown Chryco Hemi in an M37
It was time for some comedy. Friday will be my flat head 6 install into the M37day. It will be 113*F outside on that day. Luckily lots of shade, and the Porta Cool will be employed. A friend has volunteered to assist.Cal_Gary wrote:That's really clever, Outpost! I was all hyped up to see that install; however it was worth the laugh when I saw the pictures!
Gary
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- 230 engine front view with fan.jpg (111.83 KiB) Viewed 1952 times
Re: Blown Chryco Hemi in an M37
Good luck with the install. Looking at the manual starting dog on the front pulley I have to ask, Has anybody EVER started their M37 with the hand crank?
1953 M37
1964 M151A1
1967 M416
1984 M1008
4/1952 M100
12/1952 M100 gone
1964 M151A1
1967 M416
1984 M1008
4/1952 M100
12/1952 M100 gone
Re: Blown Chryco Hemi in an M37
in the spring of '69, when I was graduating from Nebraska via ROTC, and soon to be a 2nd LT, with orders to Germany, decided it was time with my (first wife, who later ran off with a lawyer when I was in SEA) , to give our MGB, so went down to the Lincoln Dodge dealer, intending to buy a 340 Dart. When I wandered around the show room, I found that a Dodge Charger R/T wasn't much more. So I ordered a green R/T, and when the salesman asked if I wanted to option the 426 for $770 more, on top off the $3275 for the R/T, I asked if it did get the Hemi, did the 440 come in a box to me to? He asked if I had ever bought a new car before to which I replied "no." I thought I would get both motors.
Soon took it to Germany, where it was just a great fast car in post-war rebuilding Germany. Sold it later to a SGT who wrecked it, I did put an Offy intake manifold on it, cutting and pasting shoe box cardboard for an intake manifold gasket. It kept working when I sold it with about 33K miles on it.
Ah, what a great car that was.
NV
Soon took it to Germany, where it was just a great fast car in post-war rebuilding Germany. Sold it later to a SGT who wrecked it, I did put an Offy intake manifold on it, cutting and pasting shoe box cardboard for an intake manifold gasket. It kept working when I sold it with about 33K miles on it.
Ah, what a great car that was.
NV
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- CPL
- Posts: 128
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Re: Blown Chryco Hemi in an M37
NAM VET wrote:in the spring of '69, when I was graduating from Nebraska via ROTC, and soon to be a 2nd LT, with orders to Germany, decided it was time with my (first wife, who later ran off with a lawyer when I was in SEA) , to give our MGB, so went down to the Lincoln Dodge dealer, intending to buy a 340 Dart. When I wandered around the show room, I found that a Dodge Charger R/T wasn't much more. So I ordered a green R/T, and when the salesman asked if I wanted to option the 426 for $770 more, on top off the $3275 for the R/T, I asked if it did get the Hemi, did the 440 come in a box to me to? He asked if I had ever bought a new car before to which I replied "no." I thought I would get both motors.
Soon took it to Germany, where it was just a great fast car in post-war rebuilding Germany. Sold it later to a SGT who wrecked it, I did put an Offy intake manifold on it, cutting and pasting shoe box cardboard for an intake manifold gasket. It kept working when I sold it with about 33K miles on it.
Ah, what a great car that was.
This is next to the M37 in the garage. '75 Duster 1969 Burnished Bronze 340 +.040" 4 speed, 3.91 in an 8 3/4" rear, Lunati Voodoo cam.
NV
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- Duster at Outpost (3).jpg (76.51 KiB) Viewed 1932 times
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- Duster at garage.jpg (104.33 KiB) Viewed 1932 times
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- Duster at Outpost (2).jpg (89.49 KiB) Viewed 1932 times