Braden LU4 Rebuild
Posted: Mon Nov 09, 2020 12:32 pm
Braden LU4 Rebuild Saga
For the four years I have had my M37, my winch has been frozen in the wind in and power out position, and would not freewheel the cable. Not a problem for me, I never intended to use it. I did fill both sides with the proper viscous oil, but it dripped out and spotted my driveway, so I drained it. Then recently I got stuck, and had to winch 25 feet out of some mud.
So, just in case I may someday have to use it again, I decided to have it rebuilt by Charles T, who has fixed a lot of things on my truck the past few years. I was about to take it up to him, when my wife told me that we needed a new dryer, and since they come as a set, got a new washer too. So…
That made it necessary for me to attempt the rebuild, and Charles T gave me advice and cautions, and suggestions for my own effort. While I have no doubt his rebuild wold have been better than Braden’s original, my goal was to make my LU4 functional for some future emergency, and not leak on my driveway.
There are some videos on this, with lots of pics, but I did not follow them exactly, using instead the Army TM’s guide. There is a lot that is not in there, by the way. And the exploded diagram on VPW’s parts list does not show one of the spacer rings, which go on each side of the “dog”.
First, I used my hoist to remove my winch, finding it easiest to remove the upper grill than the driver side bumper extension, which I had done in the past. I first powered off the cable. I still can’t really lift the naked winch, though. First problem was getting the clutch half off. The clutch “dog” was frozen on the main shaft, and the clutch shaft had a loose set screw to the fork.
I separated the clutch housing by using two hydraulic jacks, which pulled the bushing in the clutch housing out with it. Then the drum would not come off, because the keys were frozen, one broke off in it’s recess, and only by using Dry Ice to slightly shrink the other was I able to pull it out with a vice grips. (By the way, the original Vice Grips were made for decades in a tiny town in Nebraska, Dewitt, where they had a street sale once a year. )
Next, the drum was likewise frozen on the main shaft, because of rust on the shaft inside the drum. Again, used jacks to pull it off, only after using Crocus Cloth to polish the shaft. I bought via Ebay long strips of 320 to 600 grit, and used WD40, and used my diamond stones to remove the nicks on the edges of the key slots. Got the drum off, which pulled off the bronze gear on the other end; fortunately, both the bronze gear and and worm were perfect and unworn.
Next used my power washer and lots of scrubbing to clean the aluminum halves, with mag wheel etching to really get them gleaming as new, after also using stripper on the paint. When I blasted the inside of the drum, lots of oily mud came out. So scrubbed that with long brushes and assorted soaps and degreasers, even got out river sand, as if my truck at some point winched itself out from under water. I then put some Ospho rust converter in the drum, and let that dry. I polished the main shaft, and primed and painted the center section, to lessen rust in the drum section in the future. Spray painted it with several cans of 24087 after an etching primer.
I had a machine shop pull my brake gear off, and remove a few seals for me, and when a Cobalt drill and my Dremel didn’t touch the broken imbedded key, he tapped on it, and it came out in pieces.
Drove the hour to Ft Jackson, and used their shop press to install more seals. The seals for the worm l did in my own vice, with appropriate sockets. Bearings and races seemed fine, so used the gaskets as instructed to set the worm clearances, although this is done without the seals in, so pushed the new ones out, ruining them, and reinstalled another set after setting the correct gasket set. New keys for the the bronze gear, took time to press it back on the main shaft to precisely the thousandth of an inch required from the shaft end.
Found the new clutch fork was beefier than the one in my winch. One problem is that the new shift bottom seal is thicker than the old army ones, so in order to put the snap ring back on, the clutch shaft has to be some mm lower in the housing, and found my new fork’s set screw was several mm higher in the fork, so I also ground off a few mm from the pads ends of the fork arms so the whole shebang would line up the main shaft, the fork, the dog and the bushing. I reused my old fork, it was marked LU4, and the center set screw hole was an important mm lower.
Got a new clutch shaft and set screw, (NF not NC) and then used assorted grit hones, to fit the main shaft to the new clutch housing bushing. I bought Flex ones in 400-600 grits, with these many abrasive “balls” on a flex shaft, using my drill to open up the bushing just enough. From Amazon, via Zoro company.
Assembled the winch, mounted it, and it worked great, except a big leak from the clutch housing drum seal!!!! So, took the winch off again, a 15 min drill, and it was apart in a few minutes, took the drum down to Ft Jackson’s Auto Craft shop again, because the drum flanges were spread out about 3/8 inch, and thus would not let me pull the halves together enough to ensure the drum’s oil seal in the clutch housing was actually ON its drum sealing surface. Carefully pressed the drum flanges true and 3/8 inch closer, then put it all back together, but this time checked for leaks Before I mounted it. All good, so only took about half hour to mount it, and used a hydraulic jack to slightly spread the bumpers apart so I could bolt up the side mounts without cross threading one of them.
The next problem was the shifter snap ring lacked one mm of being able to snap into its recess, and the shaft could pull up and pop off the circlip due to the the thicker lower oil seal. I then used a hammer and punch on the rim of the seal just next to the shaft, and got the mm I needed to have the circlip snap into its recess.
Tested the winch both wind and unwind, the shifter smoothly moves the dog in and out. No leaks.
I hace a waterproof canvas cover which covers the whole winch, side to side, so that will lessen water intrusion. Now to rewind my cable, and hope I never have to use it again. But if I do…
And thanks to Charles T for his suggestions and cautions both via email to me, and his prior posts on this forum.
Next to put in new transfer case output seals.
All the best…. HC, aka NAM VET
For the four years I have had my M37, my winch has been frozen in the wind in and power out position, and would not freewheel the cable. Not a problem for me, I never intended to use it. I did fill both sides with the proper viscous oil, but it dripped out and spotted my driveway, so I drained it. Then recently I got stuck, and had to winch 25 feet out of some mud.
So, just in case I may someday have to use it again, I decided to have it rebuilt by Charles T, who has fixed a lot of things on my truck the past few years. I was about to take it up to him, when my wife told me that we needed a new dryer, and since they come as a set, got a new washer too. So…
That made it necessary for me to attempt the rebuild, and Charles T gave me advice and cautions, and suggestions for my own effort. While I have no doubt his rebuild wold have been better than Braden’s original, my goal was to make my LU4 functional for some future emergency, and not leak on my driveway.
There are some videos on this, with lots of pics, but I did not follow them exactly, using instead the Army TM’s guide. There is a lot that is not in there, by the way. And the exploded diagram on VPW’s parts list does not show one of the spacer rings, which go on each side of the “dog”.
First, I used my hoist to remove my winch, finding it easiest to remove the upper grill than the driver side bumper extension, which I had done in the past. I first powered off the cable. I still can’t really lift the naked winch, though. First problem was getting the clutch half off. The clutch “dog” was frozen on the main shaft, and the clutch shaft had a loose set screw to the fork.
I separated the clutch housing by using two hydraulic jacks, which pulled the bushing in the clutch housing out with it. Then the drum would not come off, because the keys were frozen, one broke off in it’s recess, and only by using Dry Ice to slightly shrink the other was I able to pull it out with a vice grips. (By the way, the original Vice Grips were made for decades in a tiny town in Nebraska, Dewitt, where they had a street sale once a year. )
Next, the drum was likewise frozen on the main shaft, because of rust on the shaft inside the drum. Again, used jacks to pull it off, only after using Crocus Cloth to polish the shaft. I bought via Ebay long strips of 320 to 600 grit, and used WD40, and used my diamond stones to remove the nicks on the edges of the key slots. Got the drum off, which pulled off the bronze gear on the other end; fortunately, both the bronze gear and and worm were perfect and unworn.
Next used my power washer and lots of scrubbing to clean the aluminum halves, with mag wheel etching to really get them gleaming as new, after also using stripper on the paint. When I blasted the inside of the drum, lots of oily mud came out. So scrubbed that with long brushes and assorted soaps and degreasers, even got out river sand, as if my truck at some point winched itself out from under water. I then put some Ospho rust converter in the drum, and let that dry. I polished the main shaft, and primed and painted the center section, to lessen rust in the drum section in the future. Spray painted it with several cans of 24087 after an etching primer.
I had a machine shop pull my brake gear off, and remove a few seals for me, and when a Cobalt drill and my Dremel didn’t touch the broken imbedded key, he tapped on it, and it came out in pieces.
Drove the hour to Ft Jackson, and used their shop press to install more seals. The seals for the worm l did in my own vice, with appropriate sockets. Bearings and races seemed fine, so used the gaskets as instructed to set the worm clearances, although this is done without the seals in, so pushed the new ones out, ruining them, and reinstalled another set after setting the correct gasket set. New keys for the the bronze gear, took time to press it back on the main shaft to precisely the thousandth of an inch required from the shaft end.
Found the new clutch fork was beefier than the one in my winch. One problem is that the new shift bottom seal is thicker than the old army ones, so in order to put the snap ring back on, the clutch shaft has to be some mm lower in the housing, and found my new fork’s set screw was several mm higher in the fork, so I also ground off a few mm from the pads ends of the fork arms so the whole shebang would line up the main shaft, the fork, the dog and the bushing. I reused my old fork, it was marked LU4, and the center set screw hole was an important mm lower.
Got a new clutch shaft and set screw, (NF not NC) and then used assorted grit hones, to fit the main shaft to the new clutch housing bushing. I bought Flex ones in 400-600 grits, with these many abrasive “balls” on a flex shaft, using my drill to open up the bushing just enough. From Amazon, via Zoro company.
Assembled the winch, mounted it, and it worked great, except a big leak from the clutch housing drum seal!!!! So, took the winch off again, a 15 min drill, and it was apart in a few minutes, took the drum down to Ft Jackson’s Auto Craft shop again, because the drum flanges were spread out about 3/8 inch, and thus would not let me pull the halves together enough to ensure the drum’s oil seal in the clutch housing was actually ON its drum sealing surface. Carefully pressed the drum flanges true and 3/8 inch closer, then put it all back together, but this time checked for leaks Before I mounted it. All good, so only took about half hour to mount it, and used a hydraulic jack to slightly spread the bumpers apart so I could bolt up the side mounts without cross threading one of them.
The next problem was the shifter snap ring lacked one mm of being able to snap into its recess, and the shaft could pull up and pop off the circlip due to the the thicker lower oil seal. I then used a hammer and punch on the rim of the seal just next to the shaft, and got the mm I needed to have the circlip snap into its recess.
Tested the winch both wind and unwind, the shifter smoothly moves the dog in and out. No leaks.
I hace a waterproof canvas cover which covers the whole winch, side to side, so that will lessen water intrusion. Now to rewind my cable, and hope I never have to use it again. But if I do…
And thanks to Charles T for his suggestions and cautions both via email to me, and his prior posts on this forum.
Next to put in new transfer case output seals.
All the best…. HC, aka NAM VET